Monday, May 14, 2012

Today we tried out our robot with the conveyor belt robot. The result was not very good. Both of our robots are complete but the programming needs to be fixed. When the conveyor robot passed ours the gate moved to far and moved our robot. Then we removed the gate and retested. The result was that the conveyor robot kept trying to keep moving even when we put our hand in front of it to replicate a gate. Other than that the robots both work well. later we fixed the gate and both robots are working better except timing is off.

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