Today was a day that did not go too well. We continued to
work on the design and found a few problems. First, the vertical design was
causing the container to become unstable. So we moved the motor to a horizontal
position and attempted to stabilize it. We found, however, that this position
was not quite working. We added a motor on the other side that might help the
robot be able to get the power necessary to work the nozzle. We also started to
work on a program for the robot to work. Our robot is still a work in progress.
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